Sure did. You have mail.
So i am seeing just under 8 psi and the truck completely shreds these tires now =). I would say problem solved.
Whipple really needs to rethink that back bolt....there is no way to get a torque wrench on it and im using a Snapon Techwrench....among others. The intercooler hoses are directly on top of the bolt due to the firewall pushing them there. I had to use a 1/4" 10 mil wobbler (small snapon chrome ones NOT the black ones) small extension and a low profile 1/4 inch rocking ratchet. I have no idea how tight i got it bit its better than it was. The socket and extension have to be slid in from the side then you can put the ratchet on...I was considering dropping the engine or moving it forward. Maybe the test trucks had higher miles than mine (1200) and the engine sags more.
Anyways, its fixed and I can move on to other mods. Next up is a bigger heat exchanger or dual 8-10" fans or both. Wonder if the mustang units are bolt on......hmmm...
Thx all.
---------- Post added at 11:49 AM ---------- Previous post was at 11:38 AM ----------
I tightened it up and retorqued every bolt I could. There is really nothing I can do about it except complain. If I bought the kit from them and not just the labor it would be different.
I know how shops work (family owns shops) and it would just **** me off. I can see getting something for free or discounted next time but nobody refunds money anymore. Its a no brainer for them "Why didn't you bring it back?" In my case they are 100 miles away and im not driving my brand new truck that far in the desert with a vac leak. Oh well =) its fixed.