GEN 2 KHC Torque Arm, anyone running it?

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Anything special we need to do to get on a list for this?

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Contact Steve @ KHC. Let him know if you're having issues and what year truck.

[email protected]



What's the fix? Redesigned bracket with clearance like mine?

Contact Steve @ KHC. As the manufacturer of the component, he can clearly articulate the fix. But essentially, what you did and increase clearance.

[email protected]




For anyone else, if you're having issues or worried you might have an issue, contact Steve! And again please let him know what year truck.

[email protected]
 

1stRaptor2019

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I talked to Steve at KHC yesterday and they are doing a modification for clearance. Not sure when mine will be delivered, but it should have the fix. He is unsure when the change on castings occurred and does not know if it is year specific yet.
 

WRCRaptor

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They are going to make a template of some sort to see if your tuck needs a new piece or can go with the old one since they have not found out when the change happened.
 

smurfslayer

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Add me to the list. I’ve been trying to do a driveway install over the past Saturday, yesterday and today ... and failed. I got all the rear pieces together and noticed I had clearance between the top cradle and the diff. Checking the front shield mount, it’s equal or slightly less space. FWIW, my truck is a 2017.

:confused:
 

lateralis

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So KHC posted it as a "story" on their Instagram. I can't find it anymore now.... Your best bet is to email them directly at the email above. I've found they respond pretty quick via email, but it's not a very good look that we haven't seen them in here since I 1st reported the issue.

Add me to the list. I’ve been trying to do a driveway install over the past Saturday, yesterday and today ... and failed. I got all the rear pieces together and noticed I had clearance between the top cradle and the diff. Checking the front shield mount, it’s equal or slightly less space. FWIW, my truck is a 2017.

:confused:

does your front diff bracket hit the diff housing? If you're concerned I'd just go straight and tell them that it doesn't fit to get that new bracket.
 
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MacK88DO

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My thought is that we now have a 2017 model with the same issue which means the likelihood of a casting change amongst model years is much less. Seems like a revised part is needed and needs to be shipped to all of us instead of a “template/cheat sheet”.


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sixshooter_45

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My thought is that we now have a 2017 model with the same issue which means the likelihood of a casting change amongst model years is much less. Seems like a revised part is needed and needs to be shipped to all of us instead of a “template/cheat sheet”.


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They didn't do their homework but should have.
 

smurfslayer

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I talked to KHC, they’re helping out.

For now, I’m going ahead without the skid plate - which I never wanted in the first place, but it was part of the group buy deal.

I want to preface what I type with all of this is because I’m not using ideal tools or work conditions for the job. Although our current house technically has a garage, previous owner built it around his boxster, so it’s a 2 bike garage - 3 at best. So this is happening in my driveway.

Doing this install in the driveway s*cs b@lls. I wish I had a lift or had just paid a damn shop to do the install. I did anticipate problems, but not THIS many. I just keep tripping over stupid stuff.

Anyway, the over the diff cradle seemed solid, I could do pull ups from it and it wouldn’t budge, but, I could verify a gap between the diff and the cradle. So, I pulled it apart, pulled the skid off and reassembled without the skid plate.

I bent the rear brake (metal) lines. I got the torque arm mounted to use the jig, and couldn’t get the damn slip joint to move, not matter how hard I hit it with the largest available implement - a 3 pound hammer. Out it comes again. With a few whacks, it comes loose, I reassemble put back in place and secure the front mounting plate. I drill 1 hole and realize the only 3/8 bit I have - I have zero 7/16 bits, is shagged. I cajole the wife to go grab 2 7/16 bits, figuring I’ll shag another one. I get a 2nd hole drilled and call it for dinner.

Let me just say, even with the new drill bits, I have new respect for Ford’s truck frames.

after stuffing my face for about 15 minutes, I got back at it and made shorter work of the remaining 2 mounting holes. So now I need to fish the 2 mounting jigs in. F***’s sake. best guess here is to fish wire through the entire width of the frame, tape to the first nut plate and gently pull through the cross frame rail. What happens? the tape stays on the nut plate when it gets in place. So, I manage to get the tape off inserting a drill bit into the nut portion of the nut plate. lesson learned. I put bolts into the nuts - this is much harder than it looks.

2nd nut plate, less drama, almost as much time. probably half an hour for each of these. 2nd Nut plate has bad threads in the nut. You cannot make this stuff up. I thought it felt tough when I test fitted, but the bolt went in, so I figured ok - good enough. <-- I should have run the damn tap through it right then and there. I fought for 75 minutes trying to get the bolt in and it just wouldn’t go. I ended up having to use the tap anyway, only while the jig is in the truck frame!

I was all prepared to drop the drive shaft for this, but, it looked like I had clearance on both sides to drill the holes, and I did. Sweet, something went right.
Wouldn’t you know, 1 of the 4 holes drifted while I was drilling. again, I fought this for 20 or more minutes until I resigned to dremeling the hole. Quoting Maxwell Smart - Missed it by THAT much. got that resolved and the t/a is test mounted and that’s where I stopped.

Hopefully, I’ll finish up soon.
 

lateralis

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Ya man those holes suck. I barely had a drill bit that was long enough to work with the tuck held up at the frame and the rear axle at full droop. I ended up leaving the arm in and wedging it up between the drive shaft to hold it in place. Did 1 nut bracket 1st than bolted it down before drilling the 2nd one to make sure it lined up. One of my nuts though got crossed threaded to hell but fortunately KHC sent me a new nut bracket and bolts.

Also it might be a good idea to get a 90 degree zerk fitting for pumping grease in at those spots. I have a straight one on my gun and its a PITA without the truck lifted and the drive shaft at full droop.
 
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