We finally had some some time to head out to the desert this weekend and take the truck for it's first real official shock testing session. All-in-all the truck worked really good. We did all the testing on the racecourse in Lucerne Valley,CA along side our buddies at Raceco-USA who were doing the same thing. For those not familiar with this section of course, it's really big holes and whoops with a good size crown down the center section of the trails. to give you an idea, our buddy with a stock Raptor was able to run the same trail at about 25mph. any faster than that, the truck became a bucking nightmare.
When we first started, the front compression wasn't near enough to handle what the back was capable of. After a few passes and getting some heat in the shocks, we ended up having to close off the long compression tube and left the short 1 turn open. It made a big difference in the balance of the truck. It wasn't blowing through the travel like when we first started out, thus allowing the front end to stay on top of the whoops better. We are going to make a compression and rebound valving change to the front end and head back out in a week or so. I'm confident that we have another 15-25% more speed once we get the front end dialed in even better than it is now. Once that is done, then we can get to work on the back of the truck. But I do have to say, the truck is amazing. It is capable of going out on the racecourse and float over massive holes at 75-80mph without feeling one bit harsh or unsettled. Also forgot to mention, the truck has our 2wd Long Travel conversion up front (18"s with Fox 3.5" Bypass Shox, and 2.5 Coilover) and our Fourlink system in the back (strapped at 24" with Fox 4.4"Bypass shox and 3.0" Coilover)
The video is a mix of onboard bumper footage with some exterior footage of showing the truck going through the same section. It is filmed in HD so make sure to click that on your youtube settings.
Thanks for watching
https://www.youtube.com/watch?v=6OeBrG2_pH8
Jarrett
When we first started, the front compression wasn't near enough to handle what the back was capable of. After a few passes and getting some heat in the shocks, we ended up having to close off the long compression tube and left the short 1 turn open. It made a big difference in the balance of the truck. It wasn't blowing through the travel like when we first started out, thus allowing the front end to stay on top of the whoops better. We are going to make a compression and rebound valving change to the front end and head back out in a week or so. I'm confident that we have another 15-25% more speed once we get the front end dialed in even better than it is now. Once that is done, then we can get to work on the back of the truck. But I do have to say, the truck is amazing. It is capable of going out on the racecourse and float over massive holes at 75-80mph without feeling one bit harsh or unsettled. Also forgot to mention, the truck has our 2wd Long Travel conversion up front (18"s with Fox 3.5" Bypass Shox, and 2.5 Coilover) and our Fourlink system in the back (strapped at 24" with Fox 4.4"Bypass shox and 3.0" Coilover)
The video is a mix of onboard bumper footage with some exterior footage of showing the truck going through the same section. It is filmed in HD so make sure to click that on your youtube settings.
Thanks for watching
https://www.youtube.com/watch?v=6OeBrG2_pH8
Jarrett