Bowewelding
Full Access Member
- Joined
- Aug 13, 2017
- Posts
- 204
- Reaction score
- 46
The first time I took the shock apart I noticed that the compression shims were double stacked so I took it down to a single "conventional " stack. The shims i had taken out I replaced the same width shims in the rebound stack to the thicker ones. I forget how thick they were now. It helped, i also flutter stacked the compression. the rebuild kits I had found ended up being the wrong kit, luckily the seal head seals fit. But the big orings that seal the body were wrong. Luckily the oem ones were still in ok shape. Im sure by now they're better kits out there but this was in 17 when we got the truck. I lowered the nitrogen level a little.. like I said before I played with the valveing but was never happy with them. I was gonna keep trying but was able to swing the kings and never looked back.. they changed the truck right away, had ordered the 3.5s for the rear but wanted to see if the dealer could figure out the advance track fault I was getting given before I cut holes in the fender well but they couldn't and thats where I'm at now..2020 with live valve. Its really nice but I still plan on changing them..just been swamped with jobs lately